The Motor Build-Up

The motor was definately a good place to begin on this project, after researching for more than a year, the block was sent to the machine shop. Here it would receive a line hone, decking, and some other small miscellaneous items. One word of caution, do not go cheap on a crank, the machinest went through 3 different cranks before he was satisfied.

The final crank was from Probe, the first two I won't mention any names here, but email me for what not to do! After many months of prep work, the block came back ready to be assembled. Thanks to the fellow patrons at Mustang Motorsports for there help with the assembly.

The rotating assembly was sent to be balanced, and ended up using a 50 oz. balancer with a 28 oz. flywheel. Again, don't skimp here! We used Probe forged pistons, Probe H-beam rods, and a Probe crank. All passed with flying colors at the shop! So spend the money up front, if for nothing but peace of mind!

I will be adding to this as the motor progresses, right now we have the motor together and the Probe pan on, Brent Frazier assembled the AFR 185 heads with upgraded valve spring last week. We have since put the heads on the motor, but no pictures yet!

...And the DART cometh?

Well the motor start-up has come and gone. And the 15 minutes of fame lived up to last winters 393 motor start-up, although this one was a bit more costly. After the first 3 runs, the passenger head was removed to see that the #1 cylinder was full of water. First thoughts were that the head gasket didn't seal, and calls were made to AFR. Upon complete disassembly of the motor, a small pinhole was found in the #1 cylinder!

So a couple of brainstorming sessions let to the fact that a broken bolt in the water pump led to the hole in the cyldiner wall. Word of caution here, when drilling out a bolt in a block, be very careful on gauging the depth of the hole!!

Instead of going with another production block and risking splitting it and being down again in 6 months, we have opted for a DART block and going to punch her in the mouth right away. So stayed tuned again, as soon as the funds become available we will be putting the 331 back together, hopefully for the last time, or at least a couple of months!!!!

Well another change of plans and the motor is back in the car as of 9/9/03. The Dart block will still be in the plans, Scott just wanted to run the car as is first. The crew at Mustang Motorsports have been busy over the weekend putting the car back together, after water leaks, fires, and unexpected down time, the car should fire sometime this week. Keep your fingers crossed. A special thanks goes out to Brent Frazier for his work on putting the motor back together in record time!!

 

 


DISPLAY:

Grey Ghost Buildup


Grey Ghost Exhaust


Project SilverFox


Blue Bomber


Red Passion


Yellow Fury


Black Night


Summer Solstice



Engine

Electrical

Suspension

Chassis

Driveline

Exhaust

Interior

Exterior

Wheels & Tires


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